Analisis Sisip Transformator Distribusi Untuk Perbaikan Overload Dan Tegangan Ujung Pada Gardu HJ177 Di PT PLN (Persero) Unit Layanan Pelanggan (ULP) Kertosono
Analisis Sisip Transformator Distribusi Untuk Perbaikan Overload Dan Tegangan Ujung Pada Gardu HJ177 Di PT PLN (Persero) Unit Layanan Pelanggan (ULP) Kertosono, Distribution Transformer Insertion, Overloadyesnd, Voltage Repair at HJ177 Substation...
Author: TRI DELLA CRISTY SEMBIRING
Date: 2024
Keywords: Distribution Transformer Insertion, Overloadyesnd, Voltage Repair at HJ177 Substation
Type: Jurnal
Category: penelitian
The HJ177 substaion in its loading datareached 126.10% (± 63,054 kVA) of its capacity of 50 kVAwith an end voltaicge of 206 V and experienced avoltage dropge of 12%. The loading exceeded the maximum capacity of the stanord transformer of 80%, which has the potential for materialand finalncial losses for PT PLN (Persero) Kertosono Customer Service Unit (ULP). The voltalge drop resulting from this has exceeded SPLNT6.001-2013 of -±10% for low voltagege. Considering the matrix in the Health Index aassessment tier-1 Distribution Transformer, willingted to the percentage of tranformer loading, it's in the bald caBeca's categoryuse it is loaded ?100%. To overcome this, an insert transformer caln be installed. With the originl load from 126.10% to 46.942% of the 50kVAcapacity, then the end voltage at the HJ177 Substation with the insertion of the transformer was originallly 206 V with avoltage drop of 12.0% increased to 213 V with avoltage drop percentage that decreased to 8.2%. The implementation of the transformer insertion for the HJ177 substation is effective in overcoming overloadyesnd improving the end voltage
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